

The first weekend in August finds us back in the little dragster at Sacramento Raceway.
This race offered 3 qualifying passes before the eliminations began.
First round of qualifying was pretty good running a 9.21. Second round of qualifying was even better at 9.18. But the third round was bad….really bad as the car seemed to have idling problems after the burn out. Randy launched the car and about 1000 feet out heard a squeaking noise and a loud clunk. Randy shut the car off and let her coast to the end. We knew watching that there was a problem also as the car blew a large puff a smoke as it rolled past the finish line.
Returning to the trailer the guys began the inspection. First item they found was the belt was missing to the oil pump, not a good sign as obviously something had gone through the pump to lock it up. Upon further dismantling of the engine to see what had happened they found large chunks of metal in the oil pan which was not a good sign either. Finally they got the pistons out and found that the number 3 piston was dead, melted, blown out and destroyed. This accounted for what went through the oil pump and the metal in the oil pan.
With much disappointment we rolled her back into the trailer. There will now be a major rebuild before she returns to the track, a new bore on the block, new pistons and sleeves and at least one exhaust and intake valve. We also need a new oil pump and get the injectors flowed.
This was the last race of the season for the little dragster so it will give us some time to get her ready for the next season which starts on January 1. Maybe Santa will bring some new pistons…if your really good.

June 19-20, 2009 - Dragster

Well I am sure that Randy will tell you that the best gift for Father's Day is a weekend of racing so that's what he got. The weather was really nice for racing low 80's and a breeze. Both Cory and Brandi spent the weekend with their dad at the track so that made it extra special too.
Although we didn't win the race we did run the fastest time yet in the little dragster a 9.01 and 148 mph. We were very excited to see those numbers come up on the ET board. In fact it hooked up so good that it picked the front wheels off the ground on the first pass Sunday morning.
It seems that each time we take it out we gain a little ground on making her run better.
Congratulations Green Motorsports...and Happy Father's Day Randy!


Brandi and Cory at the track with dad for Father's Day
May 17, 2009 - Dragster Wow is it hot! The overnight low was a balmy 65°. An early morning start at the Green house as we headed to the track around 7am for another day of racing. First round of qualifying was at 9:30am and it was already 90°. The car ran a 9.24. A very good time taking into consideration the heat we are dealing with. First round of eliminations Cory dialed the car in at a 9.24 and Randy ran a 9.26 with a good reaction time and won the round. Great job guys! After prepping the car for the next round we all tried to find shade and stay cool however possible. Cory tried to take a nap but it was to hot to sleep. We always seem to have extreme temperatures when racing, either very cold or very hot. I am still waiting for that perfect day to go drag racing! The guys say it’s always a "perfect day" to go drag racing but even they were hot! Round 2 of eliminations it was 104° and track temps over 150° but there was just a hint of air moving around. Cory changed the dial in to 9.22 and Randy ran a 9.23 almost perfect except Randy red lit at the start and was disqualified. It’s really tough to get the start right when your opposing car has a 4 second lead and your waiting on your light. But every race Randy gets more practice and experience. The car is back to running good and Cory has the dial in times nailed down so I am confident that the little dragster and Dad are going to be back in the competition by the next race.
First Round Win


Well it seems that there is always an adventure (that’s a nice way of saying something always goes wrong!) when it comes to Green Motorsports.
This is a big 3 day NHRA National Event for Randy in the dragster, Friday, Saturday and Sunday. It is also the first heat wave of the year hitting
We got to the track around 2:30pm on Friday afternoon to get the car through tech and get ready for a run of qualifying later that evening. It became apparent very soon after starting the car that there was a problem with the rebuilt fuel pump. The fuel pressure was dropping 40 pounds every time it was under full throttle. We got on the cell phones and started calling around to try to find a new pump. Finding a fuel pump to fit a dragster on a Friday afternoon is not an easy task. No one had one in town. So we called good ole' Summit Racing and they had one in there store in
burn out. The car had no reverse and the trans brake wasn’t working either. Thinking quick Cory manually held the switch on the car as they backed it up on the starting line. The first qualifying run was a 9.32 ET. After returning to the trailer they found the wires that go to the trans break/reverse buttons on the steering wheel had broken off so they were repaired. The motor was also covered in oil after the run so we tried to locate the source of the leak. They siliconed the bolts on the head and we were ready for round two of qualifying. Round 2 was much better but with track temperature at the starting line at 148 degrees it’s hard to get traction. 2nd qualifying ET was 9.24.
By the time first round of eliminations came around it was really heating up and Randy was paired with a car that was given a 4 seconds head start on the line. Randy turned the red light on at the starting line and our day was finished.
But we will be back tomorrow morning bright and early for another race in the event.
Wish us luck….we could use it.

March 15, 2009 - Dragster
Well when we woke up this morning the weather didn't look promising to get the race in. 40 degees, wind blowing and storm clouds looming overhead but we loaded up and headed for the track hoping it would clear. We managed to get in 2 rounds of qualifying and was in the staging lanes for round 1 of eliminations when the rains came. So back to the trailer we headed and loaded everything inside so it wouldn't get wet. We moved the lawn chairs inside the trailer and ate a bowl of chilli waiting for it to clear. In a little over an hour the rain drops stopped and with the strong winds it didn't take long for things to dry out enough to start racing again. So back to the staging lanes for round 1. Randy ran a slower than usual 9:30 due to the fact that the car was cold from sitting so long in between rounds but the opposing car turned on the red light at the start and Randy moved on to round 2.
Round 2 the car was running good, in fact it ran it fastest pass ever at a 9:09! A little too fast for our dial in of 9:18 but the other car ran too fast too and so Randy had another round in the win column. Round 3 they changed the dial in to a 9:08 and the car ran a very good 9:10 another great time for the little dragster but the other guy was just a little bit closer to his dial in and took the round.
All in all it was a great day of racing. We started with 40 cars in the field and made it to the top 10 and ran a new fast time for us. Congratulations Randy you made to to round 3 for the first time and had your quickest time yet.
See you at the next race on March 29th.
February 28, 2009 - Dragster

With the alcohol conversion complete we took the car to the track for some testing and tuning. Since the cars timing, fuel and all of the vitals are controlled by a computer, getting the mapping of that just right took some work. But after numerous passes and Cory making many adjustments, they had the car back to running 9.18 seconds. That is quite an accomplishment for one day.
Once again rain came in on Saturday night and the Sunday race was cancelled. The next race is March 15 so hopefully the weather will be sunny and the car is ready to compete.

February 1, 2009 - Dragster
Well we finally got the little dragster to the track this weekend. With a freshly rebuilt motor we decided to test n tune Saturday before the race on Sunday. Randy made a couple of passes and they made a few adjustments and tightened a few bolts but everything looked good for Sunday's race. Returning to the track early Sunday morning Randy took his place in line for the 1st qualifying run. Not bad at a 9.23. Second qualifying pass was better at a 9.16 but the dragster blew smoke all the way down the track all. Fearing the worst as we watched from the starting line, we jumped on the quad and went to see what had happened. After getting the car to the trailer and upon further inspection found that the oil covering the car was just because the oil was a little over filled. After wiping the car down Randy was ready for the 1st round of eliminations but on the burn out once again blew some fluids from the rear of the car (this time it was water from the overflow tank) but the crew at the track black flagged Randy for the leaking fluids and we were finished for the day. The weekend wasn't a total loss as we got in several good passes and made many adjustment to make her run better.